LTC3250-1.5/LTC3250-1.2
High Efficiency, Low Noise,
Inductorless Step-Down
DC/DC Converter
U
FEATURES
■
■
■
■
■
■
■
■
■
■
■
■
■
DESCRIPTIO
2.7V to 5.5V Input Voltage Range
No Inductors
Li-Ion (3.6V) to 1.5V with 81% Efficiency
Low Noise Constant Frequency Operation
Output Voltages: 1.5V ±4%, 1.2V ±4%
Output Current: 250mA
Shutdown Disconnects Load from VIN
Low Operating Current: IQ = 35µA
Low Shutdown Current: ISD < 1µA
Oscillator Frequency = 1.5MHz
Soft-Start Limits Inrush Current at Turn-On
Short-Circuit and Overtemperature Protected
Low Profile (1mm) SOT-23 Package
The LTC®3250-1.5/LTC3250-1.2 are charge pump stepdown DC/DC converters that produce a 1.5V or 1.2V
regulated output from a 2.7V to 5.5V input. The parts use
switched capacitor fractional conversion to achieve typical efficiency two times higher than that of a linear regulator. No inductors are required.
A unique constant frequency architecture provides a low
noise regulated output as well as lower input noise
than conventional charge pump regulators.* High
frequency operation (fOSC = 1.5MHz) simplifies filtering
to further reduce conducted noise. The part also uses
Burst Mode® operation to improve efficiency at light loads.
Low operating current (35µA with no load, 350mA, and/or TJ > 140°C)
should be avoided as it can degrade the performance of the
part.
Soft-Start
To prevent excessive current flow at VIN during start-up,
the LTC3250-1.5/LTC3250-1.2 have a built-in soft-start
circuitry. Soft-start is achieved by increasing the amount
of current available to the output charge storage capacitor
linearly over a period of approximately 500µs. Soft-start is
enabled whenever the device is brought out of shutdown,
and is disabled shortly after regulation is achieved.
Low Current “Burst Mode” Operation
To improve efficiency at low output currents, Burst Mode
operation was included in the design of the LTC3250-1.5/
LTC3250-1.2. An output current sense is used to detect
when the required output current drops below an internally set threshold (30mA typ.). When this occurs, the part
shuts down the internal oscillator and goes into a low
current operating state. The LTC3250-1.5/LTC3250-1.2
will remain in the low current operating state until the
output has dropped enough to require another burst of
current. Unlike traditional charge pumps whose burst
current is dependant on many factors (i.e. supply voltage,
switch resistance, capacitor selection, etc.), the LTC32501.5/LTC3250-1.2’s burst current is set by the burst threshold and hysteresis. This means that the VOUT ripple voltage
in Burst Mode will be fixed and is typically 12mV for a
4.7µF output capacitor.
Power Efficiency
The power efficiency (η) of the LTC3250-1.5/LTC32501.2 are approximately double that of a conventional linear
regulator. This occurs because the input current for a 2 to
1 step-down charge pump is approximately half the output
3250fa
6
LTC3250-1.5/LTC3250-1.2
U
OPERATIO
(Refer to Simplified Block Diagram)
current. For an ideal 2 to 1 step-down charge pump the
power efficiency is given by:
η≡
POUT VOUT • IOUT 2VOUT
=
=
PIN
VIN
1
VIN • IOUT
2
The switching losses and quiescent current of the
LTC3250-1.5/LTC3250-1.2 are designed to minimize efficiency loss over the entire output current range, causing
only a couple % error from the theoritical efficiency. For
example with VIN = 3.6V, IOUT = 100mA and VOUT regulating to 1.5V the measured efficiency is 80.6% which is in
close agreement with the theoretical 83.3% calculation.
0.15Ω for the LTC3250-1.5 and 0.12Ω for the
LTC3250-1.2. For a 250mA load current change the output
voltage will change by about 37mV for the LTC3250-1.5
and by 30mV for the LTC 3250-1.2. If the ESR of the output
capacitor is greater than the closed-loop-output impedance the part will cease to roll-off in a simple one-pole
fashion and poor load transient response or instability
could result. Ceramic capacitors typically have exceptional ESR performance and combined with a tight board
layout should yield excellent stability and load transient
performance.
Further output noise reduction can be achieved by filtering
the LTC3250-1.5/LTC3250-1.2 output through a very small
series inductor as shown in Figure 1. A 10nH inductor will
VOUT Capacitor Selection
The ESR and value of capacitors used with the LTC32501.5/LTC3250-1.2 determine several important parameters
such as regulator control loop stability, output ripple, and
charge pump strength.
10nH
(TRACE INDUCTANCE)
VOUT
LTC3250-1.5/
LTC3250-1.2
VOUT
4.7µF
0.22µF
GND
3250 F01
The value of COUT directly controls the amount of output
ripple for a given load current. Increasing the size of COUT
will reduce the output ripple.
Figure 1. 10nH Inductor Used for
Additional Output Noise Reduction
To reduce output noise and ripple, it is suggested that a
low ESR (
很抱歉,暂时无法提供与“LTC3250ES6-1.5#TRM”相匹配的价格&库存,您可以联系我们找货
免费人工找货